Summer 2024, Glamis gear is home. Time to get on Johns schedule and get the car to him.
Car arrives, I have a list of what it's doing and what it's not doing. John digs in and we find an ecm issue. This takes the focus away from the smoking issue for a bit. Once we have a direction on the ecm, he then see's the oil smoke. This leads into engine removal and tear down. It's got oil in all 6 cylinders and I had a burnt plug. Final tear down shows 2 collapsed pistons. John says it's heat. Too much heat. I'm scratching my head at this. How and why...
Engine gets a full refresh and installed back into the car. Off to dyno for break in and ecm fiddling. Mind you, we've consumed 4 or so weeks on this initial work, I am eager to get it back as Trey at Kali Kustoms is holding a spot for me to get the body work done on the car. Now, onto the dyno. The car has a backfire at mid rpm. This is not your little ole briggs and stratton backfire. It's a big one. Johns seeing it on the laptop and tries to tune out the noise (frequency) to get rid of it. The files in the ecm take the change, key off, power cycle etc, fire up and make a pull. Bam its back. Go back to the file and all the boxes that were checked and confirmed/saved have unchekced themselves. This goes on for a few days. AEM is contacted and with the Holley aquistion its a challenge to get anyone in that division to help. Weeks are now being counted. John is staying on it and sharing everything with me. I even reach out to AEM as the customer and give em hell. AEM sends John up and down every tree to no avail. Updating firmware, retro dated firmware and so on. Was even in a position to have to send out the ecm for repair. AEM finally stepped up with a file that had those filters locked out and John was able to install that file and get the car to run. Tuning and dyno pulls finally commence.
First good heat cycle and John finds the intercooler fan turned off. Its got power but stopped running. Couple of bangs with the fist and it turns on. That doesnt last long and its shutting off again. I mentioed earlier about John saying heat... Well he was spot on. Darn good chance the intercooler fan went to pot after the roll over and me continuing to drive the car killed the engine.
Dyno done, back to 750ish crank HP on E85.
Now its a mad dash to Kali Kustoms for the body work. We are 4 weeks behind from when I was supposed to get the car to KK.